Commit 0ceace927c ("Xilinx FPGAs: Eliminate Vivado critical
warnings", 2024-03-08) incorrectly removed the constraints for
shield_io36 through to shield_io44 (due to me applying the wrong
version of a patch), resulting in Vivado giving compile errors when
building for the Arty A7. This restores the constraints.
Signed-off-by: Paul Mackerras <paulus@ozlabs.org>
Some signals have changed names: "eth_" has been dropped from the
names of the MII/GMII/RGMII signals.
Signed-off-by: Paul Mackerras <paulus@ozlabs.org>
This resolves various warnings and critical warnings from Vivado.
In particular, the asynchronous loops in the xilinx hardware RNG were
giving a lot of critical warnings, which proved to be difficult to
suppress, so this instead makes all the xilinx platforms use the
'nonrandom.vhdl' implementation, which always returns an error.
Signed-off-by: Paul Mackerras <paulus@ozlabs.org>
The flash chip on my board is an ISSI IS26LP256P chip. The ISSI chip
requires slightly different setup for quad mode from the other brands,
but works fine with the existing SPI flash interface logic here.
Signed-off-by: Paul Mackerras <paulus@ozlabs.org>
Make the shield I/O pins be individual signals rather than a bus in
order to avoid warnings on pins which don't have both a driver and a
receiver.
Signed-off-by: Paul Mackerras <paulus@ozlabs.org>
Instead of connecting core_alt_reset to litedram init_done, it moves to
a syscon register bit. This simplifies top- files and future soc_reset
handling. sdram main.c can unset the alt_reset bit after sdram init.
Signed-off-by: Matt Johnston <matt@codeconstruct.com.au>
As with the DRAM configuration, the DC-SCM board uses the same PHY as
the Nexys Video and works with it's generated VHDL.
Signed-off-by: Joel Stanley <joel@jms.id.au>
This uses the exact same gateware as the nexys video, since the DRAM
connection is identical to the nexys video down to the pin assignments
on the FPGA. The only minor difference is that the DRAM chip on the
dc-scm is a MT41K256M16TW vs. a ...HA part on the nexys video.
Signed-off-by: Paul Mackerras <paulus@ozlabs.org>
[joel: rebase and tweaks]
Signed-off-by: Joel Stanley <joel@jms.id.au>
works with:
fusesoc build --target=antmicro-artix-dc-scm microwatt --ram_init_file=../hello_world/hello_world.hex
Signed-off-by: Michael Neuling <mikey@neuling.org>
[joel: Fixes and updates]
Signed-off-by: Joel Stanley <joel@jms.id.au>
Now that we have a 33 bit x 33 bit signed multiplier in execute1,
there is really no need for the 16 bit multiplier. The coremark
results are just as good without it as with it. This removes the
option for the sake of simplicity.
Signed-off-by: Paul Mackerras <paulus@ozlabs.org>
This is necessary for the upcoming Arctic Tern system enablement,
since Arctic Tern uses two DRAM devices and a separate clock line
is routed to each device. LiteX handles this behavior correctly,
therefore we assume other hardware exists that uses a similar
DRAM clock design.
Updates from Mikey to fix some compile issues.
Signed-off-by: Timothy Pearson <tpearson@raptorengineering.com>
Signed-off-by: Michael Neuling <mikey@neuling.org>
Orangecrab missed out on:
Make wishbone addresses be in units of doublewords or words
Author: Paul Mackerras <paulus@ozlabs.org>
Date: Wed Sep 15 18:18:09 2021 +1000
Signed-off-by: Matt Johnston <matt@codeconstruct.com.au>
Reduce litedram NUM_LINES 64->8
This allows us to meet timing. Can probably
be improved in future with better BRAM usage.
Signed-off-by: Matt Johnston <matt@codeconstruct.com.au>
top-orangecrab0.2 is a copy of top-arty with various changes.
USRMCLK is added for the SPI clock
ethernet is removed
Signed-off-by: Matt Johnston <matt@codeconstruct.com.au>
At present, code (such as simple_random) which produces serial port
output during the first few milliseconds of operation produces garbled
output. The reason is that the clock has not yet stabilized and is
running slow, resulting in the bit time of the serial characters being
too long.
The ECP5 data sheet says that the phase detector should be operated
between 10 and 400 MHz. The current code operates it at 2MHz.
Consequently, the PLL lock indication doesn't work, i.e. it is always
zero. The current code works around that by inverting it, i.e. taking
the "not locked" indication to mean "locked".
Instead, we now run it at 12MHz, chosen because the common external
clock inputs on ECP5 boards are 12MHz and 48MHz. Normally this would
mean that the available system clock frequencies would be multiples of
12MHz, but this is a little inconvenient as we use 40MHz on the Orange
Crab v0.21 boards. Instead, by using the secondary clock output for
feedback, we can have any divisor of the PLL frequency as the system
clock frequency.
The ECP5 data sheet says the PLL oscillator can run at 400 to 800
MHz. Here we choose 480MHz since that allows us to generate 40MHz and
48MHz easily and is a multiple of 12MHz.
With this, the lock signal works correctly, and the inversion can be
removed.
Signed-off-by: Paul Mackerras <paulus@ozlabs.org>
For now only the V2 of the board (slightly different pinout)
and only the A100T variant. I also haven't added GPIOs or anything
else on the PMODs really.
Signed-off-by: Benjamin Herrenschmidt <benh@kernel.crashing.org>
This makes the 64-bit wishbone buses have the address expressed in
units of doublewords (64 bits), and similarly for the 32-bit buses the
address is in units of words (32 bits). This is to comply with the
wishbone spec. Previously the addresses on the wishbone buses were in
units of bytes regardless of the bus data width, which is not correct
and caused problems with interfacing with externally-generated logic.
Signed-off-by: Paul Mackerras <paulus@ozlabs.org>
This adds an optional 16 bit x 16 bit signed multiplier and uses it
for multiply instructions that return the low 64 bits of the product
(mull[dw][o] and mulli, but not maddld) when the operands are both in
the range -2^15 .. 2^15 - 1. The "short" 16-bit multiplier produces
its result combinatorially, so a multiply that uses it executes in one
cycle. This improves the coremark result by about 4%, since coremark
does quite a lot of multiplies and they almost all have operands that
fit into 16 bits.
The presence of the short multiplier is controlled by a generic at the
execute1, SOC, core and top levels. For now, it defaults to off for
all platforms, and can be enabled using the --has_short_mult flag to
fusesoc.
Signed-off-by: Paul Mackerras <paulus@ozlabs.org>
The verilator build fails with warnings and errors, because NGPIO
is 0 and we do things like:
gpio_out : out std_ulogic_vector(NGPIO - 1 downto 0);
Set NGPIO to something reasonable (eg 32) and add HAS_GPIO to avoid
building the macro entirely if it isn't in use.
Signed-off-by: Anton Blanchard <anton@linux.ibm.com>
Experimenting with using ghdl to do VHDL to Verilog conversion (instead
of ghdl+yosys), verilator complains that a signal is a SystemVerilog
keyword:
%Error: microwatt.v:15013:18: Unexpected 'do': 'do' is a SystemVerilog keyword misused as an identifier.
... Suggest modify the Verilog-2001 code to avoid SV keywords, or use `begin_keywords or --language.
We could probably make this go away by disabling SystemVerilog, but
it's easy to rename the signal in question. Rename di at the same
time.
Signed-off-by: Anton Blanchard <anton@linux.ibm.com>
The icache RAM is currently LUT ram not block ram. This massively
bloats the icache size. We think this is due to yosys not inferencing
the RAM correctly but that's yet to be confirmed.
Work around this for now by reducing the default size of the icache
RAM for the ECP5 builds.
On the ECP5 85K builts, this gets us from 95% down to 76% and helps
our CI to pass.
Signed-off-by: Michael Neuling <mikey@neuling.org>